Showing posts with label DIY. Show all posts
Showing posts with label DIY. Show all posts

Friday, March 28, 2025

Best before dates

 

PVA glue
According to the top of the bottle, the big one here was made 03.11.2021, and the small one 03.12.2024. 

And on the back, it says that the shelf life it 12 months from date of manufacture. Interesting. The big bottle is past its best, and we have a couple more that are pretty poor now. 

I'd never really thought of PVA having a "best before" date, but there's obviously something in it. From now on, 500ml is enough, I'll probably use that up while it's still at its best. And if I don't, well, the stuff is cheap enough, and the next bottle will be good for 12 months too!

Monday, July 26, 2021

Hozelock reel frustration and resolution

 

This is a Hozelock retracting reel. It's a nice, neat way to have a hosepipe, and gave me a whole heap of pain on a very hot Saturday, trying to fit to the wall. Definitely one of those jobs that looks simple and descends into a nightmare. 

In theory, all you do is drill four holes, pop the rawplugs in, screw the support to the wall and it's job done. 

Of course, you have to get all the holes in the right place, and that's tricky as the plastic bracket gets in the way of marking things. 

The solution - make a cardboard jig. 

Ideally, do this before drilling a series of wrong holes and using up all the plugs supplied. 

This reel is heavy. 17kg as supplied, but it will get heavier when full of water and then even worse - it's the ideal perch for next-doors cat, and he's not small. 

So, you need really strong plugs. The ones in the kit have little barbs. 

None of the plugs in our garage had these, so when we hung the support on the wall and fitted the reel, they started to pull out again. I'd put all the supplied ones in the wall, so couldn't take one to the local DIY shed to try to find a replacement. I went anyway, and nothing they had in the very limited stock, was any better. 

Fortunately, Hozelock sell spare packs, and I don't care they are six quid for four screws and four plugs, I bought two. Delivery was quick, and the reel was soon fitted to the wall. So far, it hasn't fallen off, although one of the very long screws supplied has bottomed out in the hole, but it's at the bottom so doesn't seem to be effecting things at the moment. 

Fingers crossed, and let's hope the cat doesn't put on any weight...

Sunday, July 11, 2021

Painting the dragon

I wasn't confident I would have enough plants to fill my garden railway display and decided a little more colour would be useful, and ideally, something amusing. 

Our garden is home to a number of concrete ornaments, normally nicely painted by myself. I use cheap acrylic paints, the sort bought from The Works for a quid a bottle, and even though these figures live out all year, the paint usually lasts for three, before they look tatty. It then takes at least another two for me to do something about it. 

The little dragon climbing out of a manhole cover was well overdue for refreshment, and since he occupies a reasonable area, but without being too tall, I decided that his time had come to make a public appearance. He's always been one of my favourites too. 

An hour of painting with cheap brushes and some sponged highlighting and he really looked the part. The paint needed a little thinning for the black cover to make sure there weren't any bald spots, but basically, I squirt it on a plastic lid and use straight from the bottle. 

Although around the back of the display, a few people spotted him. Maybe I'm not taking the hobby properly seriously, but then I think it's all about having some fun!

lthough around the back of the

Thursday, March 04, 2021

Fixing the front door lock

I like taking apart mechanical things, especially those with chunky fixings. When the catch on our front door stopped working properly, after being allowed to slam shut in the wind a few times, it needed investigating. 

OK, it needed replacing with an identical one, but after that I took the old unit and had a play. 

The basic device is simple enough, there's a bit that turns which shoves a cage back and forth, on to which is fitted the brass tongue bit that locates in the other side of the unit to hold the door shut. Obviously, I've not looked up the correct technical terms...

The fault was that every so often, the handle inside the door seemed to lose contact with the slidy cage and flop around. My first thought was that the cage could move out and miss contact, but there didn't seem to be a problem there - no obvious wear in the plates holding the thing together, and the two, chunky retaining screws were tightly fitted.

Eventually, after about half an hours tinkering, I spotted the cage was slightly distorted. Slamming the door on the latched unit had whacked the tongue and moved the metal. Five minutes with pliers (it's quite soft) and a hammer and the whole thing moves silky smoothly. As good as new. 

Now, we have a spare front door lock all parcelled up in the garage, where it will probably manage to vanish if we ever need it. 

Anyone else like this sort of job?

Friday, October 09, 2020

The most satisfying job of the day

 

A couple of weeks ago, I wasn't having a good day. Every so often, the news really gets me down and I can't concentrate on anything useful for work. Trying to do some modelling, or pretty much anything isn't going to happen, but I was lucky, there was one job that I was confident I could do. 

My sister has a shed/studio at her cottage and one of the windows had broken. She had specified a plastic replacement and a sheet was ordered from the same shop I get my baseboard wood from. 

I picked this up along with a couple of lengths of quarter-round strip. Oh, and some pin nails as I'd forgotten to pack some. These, and some tools, headed to her place and within 20 minutes, the hole was filled. Quite nice and neatly too. 

Oddly, it was a really satisfying job. Not difficult to do, but definitely "a good job done". We all need this sort of task occasionally I'm sure. I know I did.

Thursday, August 06, 2020

Dual-flush cistern bodging

Is there anything more annoying to not work at home than the toilet cistern?

Most bits of house equipment can be worked around, but we all need to poo!

So, when our dual-flush cistern decided that it would keep filling rather than filling and stopping, repairs had to be effected quickly.

The problem was that the seal on the bottom of the flush mechanism had hardened a little and couldn't be relied on. Wiggling the unit with every flush fixed it, but was hardly ideal.

Since I was up to my neck in Virtual Show, my dad called a plumber. He had a look, said it would take a week to get the bits and left leaving a quote for £70. This seemed a bit rubbish - I'd expected to see a van with spares in it, not a car for a start. There is a reason he was available the same day.

Anyway, I left the computer for a while and had a poke around. The flush unit is separate from the inlet, so with the water turned off at the in-line valve, and a Readers Digest book of DIY to hand, worked out that twisting the unit would unlock it from the outflow and it was lifted away. This is how I found the hardened seal.

An hour later, dad was back with a complete replacement unit, price £27. Not a week, an hour. Parent 1: Plumber 0

I put the new unit in place and hoped all would be well. It wasn't.

There were two problems. First, the flush wasn't particularly powerful and worse, the clip that connects the control cable to the button, kept falling off.



The design of the clip is rubbish. It hangs limply on the bottom of the button. I tried swapping parts around with the old unit, and in an unexpected twist managed to reverse the direction of the cable so it no longer tangled with the inlet valve. This didn't help much, but I was pleased.

Anyway, I worked out that a screw passing across the edge of the connecting hole would tighten things up - and after some careful drilling, screwing and adjusting, this worked. The clip stayed put. Result!

The flush was still a bit rubbish, but I had a plan. You see I'd worked out this set-up wasn't very good and headed online to see what the alternatives were. Ideally, I wanted something that didn't need me to get at the bottom of the cistern because the design of this toilet covers it up. Removing the cistern would be doable, but more time and trouble than I could do with.

What I found, from the very helpful Plumbase, was the Wirquin One. According to the instructions, and videos, the unit takes about a minute to fit. It twists into the fitting in the bottom of the cistern (check this, they vary, there seem to be 2 or 3 designs) and then sits under the button hole.

The unit arrived and I fitted it.


Fitting is indeed quick. Set the flush levels (Max power!), unscrew the button. Pull the cage thing up and put the lid on top. This pushes the cage down and puts the screw thread right under the button hole.

Screw the button in place and flush away. Job done!

OK, it took three goes before I was happy. Every so often, including 2:40am, the unit wouldn't seal and the filling carried on, flowing straight through the unit and into the bowl. Grumpy face.

I rang Wirquin and they couldn't help, recommending I reinstall the unit. A bit like being told by IT to turn your computer off and on again. I did this three times and now (fingers crossed) we seem OK. Lots of flush, although when you release the button, not when you push it, and a reassuring slight "whump" noise after the flush that indicates the unit has sealed and will let the cistern re-fill. Reassuring in the same way a solenoid point motor is when you know it's gone across. I like reassuring noises.

I like toilets that flush as well. I'm giving this thing a fortnight, if it works, all the old cistern mechanical stuff goes in the bin and I'll buy a Wirquin spare unit. It's a lot cheaper than a plumber. Even one neither surprised or bothered when he is cancelled.

Monday, August 05, 2019

How to change the wheel on a wheelbarrow

My Mum's wheelbarrow has a knackered tyre. Years of living outside and being used without the correct amount of air in it have killed the rubber. The wheel itself is OK, but replacing both is a lot easier. We couldn't find a tyre on its own anyway.

Step 1: Oiling up


Unless you treat your barrow with the reverance normally applied to a classic car, the bolts will be rusty. Spray with penetrating oil and go and make breakfast. Spray again and go for a cup of tea. Clever people will spray and leave overnight, this stuff is good, but needs time to work.

Step 2: Unbolting


One side of the bolts has a 13mm nut, the other a pointless slot in the head. No screwdriver is going to hold the head when the presure is applied, but a set of molegrips will do the job. It's time for brute force! Actually, thanks to the oil, the bolts undid pretty well.

Step 3: Remove the axle


Engineers will say they "drift the axle out", I just whacked it with a mallet as the new wheel doesn't come with one. A shot of the penetrating oil isn't a bad idea before you start belting things, although this one wasn't a tight fit. There are two spacers lose, one either side. Don't lose them.

Step 4: Reassembly


Clean and grease all the bolts and carefully put everything back together. Then remember the spacers on the axle, take it all apart, put them in and reassemble. Make sure the U-brackets are the right way around. Grease between all the metal-to-metal joins in case you want to do this again in the future, but wipe all excess grease away as it will attract dirt.

Step 5: Pump up the tyre


Use a footpump to inflate the tyre to whatever it says on the side and then the barrow is ready for use. Buying new barrows is a hasstle (they don't fit in the car very well) and chucking an otherwise servicable tool away a waste.

The new wheel came from Torrys Hardware in Warwick. If you manage to get just a tyre, the steps are pretty much the same, you just need to remove and replace the rubber bit as well.

Friday, September 21, 2018

Harris "No Loss" brush review

Faced with a "garden room" (posh shed) requiring a coat of yacht varnish before winter, I headed to the local DIY store for some new brushes.

I've always been pleased with the Harris "No Loss" range. Unlike slightly cheaper brushes, they don't seem to moult hairs as you paint. To be fair, they are better described as "a LOT less loss" and on the shed, I reckon I lost about 4 or 5, but then it's big enough to need a full large sized tin of varnish, so that's not bad going.

It was certainly a lot easier than picking bristles out of the varnish. That game gets old pretty quickly and you end up trying to shove them somewhere they won't be spotted rather than experiencing another dose of sticky finger bristle picking.

The only disappointment is that some muppet has re-designed the handles to be a bit more streamlined. Very pretty, but the end is now quite a bit sharper than it was before and once you hold it half way down the handle for fast application of lots of varnish, it digs in your palm. The old, blunter ones didn't do this.

Overall though, they are well worth the money. I've given a old set lots of stick and they still work OK. It's worth taking time to clean them properly, but even there you don't pull out handfuls of hair, which makes a messy job a little more pleasant.

Tuesday, March 13, 2018

New broom? You'll need someone with a toolbox...


OK B&Q - the yard broom at chez Parker is looking more than little tired. To be honest, it lives outside the back door and the wood has gone rotten. Trying to sweep the recent fluffy snow away before it turned to ice defeated it.

However, the packing for new brooms presents a challenge. The head comes attached to the handle with this plastic bracket.

You can't slide the handle out, the prongs prevent easy movement and when you reach the end of the handle there is either a bit of rope for hanging the broom up, or the plastic thing that screws into the bracket on the head.

Cut that away with some flush wire snippers and you are left with the plastic bracket stapled to the head. A screwdriver won't go in under the staples until all the plastic is cut away with a Stanley style knife. OK, it's pretty soft but so is the wood underneath.

And those staples are long too.

Anyway, the broom is now assembled, plastic bits and staples in the bin, and treated to a coat of varnish ready to go outside. It just seemed to be more of a faff than it ought to be.

Thursday, January 11, 2018

Building a childs wooden multiplay playhouse

Recently, I offered to help assembled a TP Wooden Multiplay Playhouse for a friend's 4 year old daughter. Being told that it was a wooden garden toy that came in pieces, I couldn't resist the chance to get involved.

Before getting started, I asked for the details I could pack a suitable toolkit. This photo duly followed:


Not too bad. I added some glue and sandpaper to the box. Looking at the reviews, these seemed positive with the fastest build time being 3 hours. This mattered as we planned to start at 2pm and the daylight deserts us around 5pm. My favourite was the "we got a box of sticks and had to pay someone to build it for us!!!" one - what exactly did they expect?

To help me, I enjoyed the assistance (or maybe I was the assistant) of the recipients grandfather, an engineer who enjoys some seriously high-quality woodwork. He also arrived with a more generous toolkit than the instructions suggested. We've both been caught out before...


Construction started well. The basic platform went togehter easily enough. There are a few things to pay attention too - the floor isn't in the middle of the uprights so you need to make sure you have everything the correct way up.

Most of the holes are drilled which is a massive help, but the screws are sometimes long - up to 16cm in several cases and my Bosch cordless screwdriver wasn't quite up to the job. Fortuantly, John's version was rather more powerful, saving loads of time, even if it didn't allow him to use his collection of Yankee screwdrivers very much.

We made a couple of mistakes along the way - the floor planks have cut-outs for the corners and so these were pushed well in leaving a lip along the edge over the main beams. This is wrong and we had to undo a little work to shove the planks over. Not a biggie.

We also (OK, I also) got a bit confused attaching the outside plank walls and managed to build one 90 degrees from where it should be. As it happens, this only required the removal of one long plank and it's replacement with a short one.

I enjoyed the build. It went together well, but you have to pay attention as you go. John insisted on being properly precise, marking wood with both pencil and square so we lined things up properly.

Build time was 2.5 hours - a world record but we don't want to boast about it. To be fair, the 2 cups of tea and 1 of diet coke were drunk as we worked so no breaks for us.


One modification we made was to fill in a hole in the side with a bit of spare plank (you can chose where the slide exists and have to shorten a plank to do this, leaving a bit of spare wood). It's not high and any landing would be on grass, but it's better to keep small children inside.

The big mystery is, why did we need spanners? There were no nuts and bolts in the pack and no indication any optional parts that would use them. (Update: The same tool list is in the swing set instructions as well and this DOES use bolts - presumably it is a standard graphic used for each set of instructions.)

If you are contemplating a build like this, get a massive cross-head screwdriver and a really powerful screwdriver. Ideally, you need 3mm drill bits about 6 inches long but we managed with normal ones - just.

The kit is well designed and all the parts numbered with little stickers that you can see on the finished building. Some de-stickering work there for Mum I think.I'm told the little one is thoroughly enjoying it though, so that counts as success.

Monday, March 13, 2017

Dust and muck


I can't stand seeing people messing around with the wrong tools for the job, especially when the right tools are easily available.

Which is why I confiscated the rotating brush head from our Henry vacuum clears from my dad as he prodded and poked at it with a large screwdriver. It might have been the right tool for undoing the screws holding the two halves of the casing together, but not for de-fluffing the inside.

Carefully stripping down the mechanism was great fun. The fan blades which drive the brushes were removed using a vice and large hammer gently applied. Fine pliers pulled out rubber mounts and gradually extracted all the muck from inside.

Eventually it all went back together. Sadly, to no great effect. The cover over the drive belt has worn through in two decades of use and jams the unit so it looks like time to go and buy a new one. Still, taking things apart is fun!

Sunday, January 08, 2017

Appliance repair

From xkcd earlier in the week.


Across the world, tinkering types recognise the problem and are nervously laughing...

Monday, December 26, 2016

Rock stand


All being well, my sister is now the proud owner of a lump of rock. I'm not exactly sure what sort of rock it is, and probably wouldn't spell it correctly if I did, but it's a really nice and interesting green colour. 

It's also an odd shape, which made the request I built a stand for it to sit on a bit of a challenge. A bit of web surfing provided some ideas, but most of them didn't seem quite big enough, or I had to buy the things in bulk. I reckoned that I could make one myself however. 


The wooden base came from eBay, a nice piece of oak for a few pounds. The 4.5mm diameter brass rod is from Eileen's Emporium. This cuts well with a tube cutting tool, you even get a nice chamfered end that only takes a tiny amount of cleaning up with a file. 

The rear support was bent in a vice, not as neatly as I'd have liked (it looks worse in the photo) but as this is hidden by the rock, I could live with it. Holes needed to be vertical so I dug out the pillar drill. No glue required, just firmly pressing the rods home with a vice or long clamp. 

Finishing touches involved Brasso and some metal lacquer to save future polishing. 
 

Tuesday, November 29, 2016

Softening PVA glue joints


My dad's Bismark project continues with the odd instruction to sand 2mm from the side of each aircraft hanger.  These were assembled some time ago, so I assume this modification is an error in the original parts spotted late in the day when producing the series. 

Losing 2mm from a pieces of MDF is some serious sanding and almost impossible to achieve accurately without mechanical help. Far easier is to replace the part with a new one the correct thickness. The Parker stash of thin wood is well stocked with suitable material. 

The only problem is that the parts are fixed together with waterproof (blue bottle) Resin W. 

No matter, leaving small pads of damp kitchen towel against the joins seems to have weakened them enough that the sides to be replaced could be gingerly peeled away. I'm not sure that the glue has been broken in all cases, but the join softened enough that the very top surface of the MDF was peeled off.

Friday, November 04, 2016

Shower stripping


Last Monday, our electric shower suddenly stopped working. Water came out, but it was cold. The lights were on, it had worked perfectly well the day before, but not now.  This makes me grumpy - the day never seems to start well if I can't have a shower.  

Anyway, a local plumber had replaced it by the end of the day for a very modest £150. For the purposes of this blog, I ought to claim to have done it myself but water and electricity aren't happy bedfellows so I prefer to leave well alone. More to the point, if the inlet isn't in exactly the same place then plumbing is required and probably fittings the man will have on his van and I'll have to go and buy. Stuff that. 

The old shower was dispatched to sit on the top of our green recycling bin in the back garden. A couple of days later, I took a look and spotted the on/off switch. It looked interesting and was fitted with a couple of reasonable sized cross head screws. 

20 very enjoyable minutes later, I'd retrieved the switch, a couple of microswitches and a few other bits. It was a pleasantly warm day and I was undoing screws in something I didn't need to put back together. I didn't really need to undo as many as I did, but I was having fun. 


Out or curiosity, I had a look in the "boiler" bit. That's where I suspected the problem lay and I wondered how it worked. 

Opening this up took a bit more effort - specifically chopping the plastic body in half with a hacksaw. Inside there are two heating coils. Turning the power switch makes each live in turn. That's why there are 2 microswitches operated from it. I still don't know what's wrong, but it was fun finding out. 


By the end of the dismantling session, I'd amassed a little pile of bits. I'm not sure what a couple of the round ones are but hopefully a multimeter will tell me more. 

The rest is probably junk, although that mahoosive choc block looks useful. The bigger screws aren't self-tappers but have coarse enough threads that I reckon they can be forced into suitable pilot holes. The shorter ones are anodized a copper colour and just looked pretty. 

This ought to be a piece where I buy the parts and repair the shower. It's not, because I didn't fancy trusting my skills where potentially deadly forces are mixing. That and delivery takes days and I wanted not to smell bad. As it is, the resulting landfill pile is much smaller than it would otherwise be and I've got some new bits to add to the box of miscellaneous electrical parts already rescued from other places. Hmmm.



Saturday, August 13, 2016

It just needs a bit of T-Cut...


After a slightly random conversation at the model boat club, I find myself custodian of this GWR station lamp. The previous owner had inherited it and didn't want to throw it away. He had no desire to  own a rusty relic though - so passing it on to me for free solved all his problems. 

I can't resist a bit of railwayana but this isn't without it's issues. The main one being that quite a lot of it is composed of rust. The frame around the glass is OK, but both the bottom and top are basically knackered. 

Sensible people would throw this away - or at least find some other numptie to pass it on to. 

I'm not sure what to do. Replacing all the rust wouldn't leave much of the original. There's little metal to weld to so replacing rust with steel isn't likely. My initial thoughts involve some automotive glue. Maybe if I stabalise the rust, I can glue metal inside the rotten bits. 

Dunno. For the moment it's in store while I think. Suggestions welcomed.

Monday, July 25, 2016

A happy customer service story


Let's start the week with a happy story (SPOILER ALERT - everything works out fine). 

On the back of our house is a waterproof socket. It's the second one to be installed, the first having rapidly fallen to bits because the electrician brought in to fit it bought cheap rubbish. This one works much better, is easier to close and generally is good. 

Last week, one of the grey catches that clamp the  door shut broke. 


Looking at the (paper) catalogue, these clips seem to be common to several sockets so I wondered if I could get a replacement. Ringing the number on the book didn't work (always engaged) but a Tweet sent to @Screwfix got a response within 20 minutes.

After direct messaging them with the order details, and I didn't have the number, just the date of purchase and my address, I received a phone call - at 8:10pm. This was a surprise but welcome and Audrey explained that if I dropped into the local branch they would try to help. She also e-mailed me the original order so to make things easier for the branch.

The next day I explain the story to the local people who do their best to extract a good clip from a socket in stock. This proves impossible (you need a tiny punch to remove the hinge pin, hardly a common tool) so we agree that if I buy a new socket, I can go away and use the entire front panel, then put the broken one in the box with all the other bits and return it for a refund.

8 simple screws later, the new door with 2 working clips is installed - no need for an electrician as I didn't disturb any wires (still switched it off at the distribution box though) and all was well.

Finally, everything was boxed up and returned for the promised refund.

All in all, excellent service. So good, I felt I wanted to write a blog about it to say thanks to everyone who helped.

Monday, December 14, 2015

Fixing footwear


I don't like things I can't repair. One pet hate is those stupid plastics that don't react to any known glue so once broken, can only head towards land-fill.

Another issue is shoes. Occasionally, the sole starts to come unstuck from the top and needs a little glue to fix the join. It was glued originally so repair ought to be easy.

Trouble is, the join has to flex. You can't use epoxy as it's too stiff and after a few feet of walking, starts to break down. Evo Stick, being a rubber glue, ought to be better but never seems strong enough to me. I'll confess that I've even had failures when having repairs professionally carried out. New soles pulling away from perfectly good uppers for example.

A while ago, I bought a tube of Unibond EXTREME glue. It claims strength and flexibility so I gave it a go.

I can report that on one pear of shoes, the join, at the toe, was effective and allowed me to cover many more miles before I wore the soles out. More recently, it's been used to re-fix a boot sole which shows no evidence of glue being involved in the manufacture and this seems OK.

Two tricks: Open the gap with a screwdriver so you can squirt the glue well into the join. Second, a paper towel dampened with white spirit wipes away splurges of glue from the sides, leaving a perfect join.

Saturday, August 22, 2015

Pipe repair

 
Maybe repairing a Dolphin Pools pipe fitting isn't the most common reason to be reading this blog, but I think the fix is a bit nifty.
 
The problem was that the vacuum suction cleaner pipe for the pool was breaking up along the bottom edge where it plugs into the outlet to the pump. Gaffer tape had kept it going for a while but eventually the cracks became too large.
 
A trip to the pool bits shop revealed that the paart is no longer available - indeed the guy in there is trying to find replacements as several customers are looking for one. The mix of chemicals and UV light aren't good for the plastic obviously.
 
Anyway, a few minutes with some calipers established that the outside diameter of the connection was about 1/2mm larger than the inside diameter of plastic waste pipe. Grabbing an offcut from the garage, with a bit of shoving it slid perfectly over the broken section. A splodge of pipe adhesive solvent and the section is braced with a sheath of pipe.
 
It still clips into place but should last another few years.

Saturday, June 27, 2015

Super cheap clock repair


Years ago, I bought a computer monitor shaped clock from someone on eBay. I've always liked clocks and have to stop myself building a vast collection of them in all shapes and sizes.

The Nokia monitor is only 10cm wide and sits on a shelf by my real computer. When I first bought it, monitors were this shape. Now the one I type on is thinner than the clock!

Anyway, given out as a freebie at some show, it wasn't built to last and the mechanism stopped working after a couple of years. Sensible people would throw it away but I'm not, so I didn't.

Instead, during a recent trip to Ikea, I bought a VÄCKIS alarm clock for the breathtaking price of 80p. I don't even want to think how they produce something with mechanical bits so cheaply...

(I tried the "Ask Anna" link on the page by the way but she wasn't very helpful on this point)

 
Taking both clocks to pieces was a matter of some cross head screwdriver work and prising the clear plastic out of each gently with a tiny, tiny, screwdriver under the edge. Hand and adjusting knobs bulled off the back of each.

Sadly, the Nokia hands won't fit the Ikea mechanism but its own hands don't look too bad.

 
Neither clock uses a screw in holder around the hands. The Nokia clips into place behind the face. As Ikea don't use the same clips and their mech is slightly smaller, I put a couple of dots of superglue between face and black plastic casing and then wedges some 1mm thick plastic sheet behind the clips to grip the part firmly.
 
After this, the face is clipped back on its body and all is well again. There's even so much space in the monitor that the old mechanism can be tucked in there in case this turns out to be a rare collectable and needs to be restored.